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<br />nitrate is 10 parts per million (ppm). Well #3 has tested as high as 9.0 ppm and Well #5 <br />has tested as high as 8.2 ppm. <br />The water quality and production study that was completed this past spring <br />recommended blending water from a new well to lower nitrate levels in Well #3. <br />However, the two test wells drilled showed nitrate levels of 6.5 ppm and 7.0 ppm; too <br />high to effectively blend. As a result, staff is proposing to construct a treatment facility <br />that would lower the nitrate levels at both Well #3 and Well #5 to below 5 ppm, which is <br />comjarable to the water quality from Well #7 (Roadside Park tennis courts) and Well #4 <br />(23r St. near the Hastings Country Club). The blending of water from Well #3 and Well <br />#5 for nitrate removal will have the added benefit of reducing the levels of cyanazine in <br />the end product well below the most conservative health standard. <br />The remaining well, Well #6 (Spiral Blvd.), has spiked above 10 ppm, but <br />generally has been running with nitrate levels bouncing between 5.5 to 6.5 ppm, with the <br />nitrate levels showing a slow but steady increase. A future decision will need to be made <br />about construction of a second nitrate treatment facility at Well #6 to remove nitrates <br />from water pumped from Well #6 and Well #8. <br />Construction of a treatment facility for Wells #3 and #5 will also include <br />construction of a new trunk watermain and raw watermain between the two wells, <br />improvements to the booster pump system at Well #5, modifications to Well #5 and <br />pumphouse, additional piping changes, improving the interconnection between the low <br />system and high system at the Well #5 site, and major control system improvements. The <br />preliminary cost estimate for the treatment facility is $2,200,000. The trunk and <br />interconnection watermain cost is preliminarily estimated at $800,000. The well, piping <br />and control system modifications are estimated at $700,000 for a total cost of $3,700,000. <br />As proposed, the interconnecting watermains would be constructed next summer. <br />The treatment facility would be designed this winter, with construction to begin in the <br />spring of next year and completed and operational by the spring of 2007. <br /> <br />Fundin2 <br />The preliminary estimates for construction of a new well and a treatment facility <br />total $5 million. The City has a $1.7 million balance in WAC fund. WAC funds are <br />. collected on building permits for new construction to fund expansions to the water <br />system caused by growth. The City also has a $2.7 million balance in the Water fund. I <br />would recommend retaining a minimum reserve of $1 million for emergencies and cash <br />flow balancing. This leaves a total of $3.4 million of cash on hand. <br />However, there are other water systems improvements planned for the near future. <br />The cost of a downtown water strengthening main that would be constructed as part of <br />the riverfront redevelopment is estimated at $500,000. Earlier this year, Council was <br />presented information about a long range plan to address fire flow deficiencies in the low <br />system by constructing trunk watermains that would loop from the Tilden School area to <br />the Downtown and south from the Downtown to complete the loop at CR #47 and Hwy <br />61. Staff will soon propose reconstruction of 3rd Street for the 2006 improvement <br />program, which will include part of the above described water improvements to address <br />fire flow deficiencies. At this time, I do not have a cost estimate for these phased water <br />system improvements. As growth continues, the City will need to construct additional <br />wells and water storage tanks. <br />